| By Jesus Diaz How a Captain Got Sucked Out Of a Blown-Up Cockpit Window and Everyone Survived
That's exactly what happened to Tim Lancaster on flight BA5390, when he was piloting a 43-tonne British Airways BAC 1-11 airliner at 17,000 feet, on June 10, 1990. Fortunately, Nigel Ogden—a flight attendant who was getting out of the cockpit when the windshield blew away—didn't lose his cool. As the explosive decompression "made the whole cabin mist up like fog for a second" and the "plane started to plummet", Nigel thought it was a bomb. Later, it was discovered that the cause for the explosive decompression was an improperly installed window pane, which has been replaced 27 hours before the flight. When Nigel turned around, the scene was terrifying:
Soon, the pressure equalized, but Tim was still out of the plane and the wind start getting in the cabin at about 630km/h (391mph) and -17ºC (1.4ºF). The co-pilot struggled to gain control of the plane and he did it, taking down to 11,000 feet in two minutes—where there was more oxygen. But Nigel was still holding Tim and the situation was still critical. The plane may have been stabilized, but the captain was still hanging out of it.
Amazingly, with the help of another flight attendant, they were able to pull him back. And even more amazing: Tim as more or less ok, frostbitten and with some bones fractured, but alive. In fact, back in 2005 he was still in active, flying for EasyJet. The BA plane landed without any other problem—even while they feared that a catastrophe could happen if there was more damage. It was 07:55. Only 18 minutes had passed from the explosive decompression till the planed landed on Runway 02 at Southampton Airport. To everyone in that cockpit, it felt like hours. Read the whole account as told by Nigel to Julia Llewellyn Smith in the Sydney Morning Herald. [SMH and Wikipedia via The Atlantic] | April 6th, 2011 Top Stories |
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